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Wagenman 29-32 #1H

File #22057 | Devon Energy Williston, LLC | Williams County County
API
33-105-02477
Target Formation
Middle Bakken
Permit Explained
Yes

Permit Cycle Assessment

The permit action is a routine change of operator. The Industrial Commission approved the transfer of the well from Grayson Mill Operating, LLC to Devon Energy Williston, LLC effective October 31, 2025. The transfer was properly noticed via Form 15 and the well is now covered under Devon's bond. No operational or regulatory conditions were modified; this is an administrative ownership transfer.

Permit Cycle Signals (1)

Change of Operator from Grayson Mill Operating, LLC to Devon Energy Williston, LLC (2025-10-31)
Industrial Commission approved transfer of operatorship to Devon Energy Williston, LLC with bond coverage under Bond No. CMS0358791 effective October 31, 2025

Historical Non-Routine Signals (3)

Stripper Well Property Determination dated May 11, 2022 (2022-05-11)
Well qualified as a stripper well property with average daily production of 27.5 barrels during the qualifying period (February 1, 2020 through January 31, 2021), which carries ongoing tax implications for the operator
Commingling authorization with Wagenman 29-32 #2H (2012-08-13)
Wells use continuous measurement at a double pad facility with allocation methodology specified for oil, gas, and water production reporting, affecting ongoing production accounting and regulatory compliance
Confidential status granted for six months from spud date (2011-12-13)
Historical confidentiality period established the initial data disclosure timeline, though this period has long expired and well data is now public

Historical Operator Profile

Total Wells:N/A
Active Wells:N/A
Notable Patterns:None identified

Confidence Assessment

Level: High
Rationale: The permit action is clearly documented with explicit approval letter from the Industrial Commission dated October 31, 2025. The Form 15 transfer documents, bond information, and effective date are all clearly stated. Historical context is well-supported by dated correspondence and regulatory filings spanning the well's operational history from 2011 to present.